Today for open lab we fully tested the new back wheel we added.
In addition to this changed we have also made some maintenance after an incident that occurred when testing. We have realized that the previous team did not follow the instruction to the best capacity. Today we fixed the an arm problem that made the arm temporarily motionless. we did this by tighten lose parts
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Dewey - Tell Me About Your VEX- Pinned Post
VEX Robot's Resource Page If you are in my Mechatronics Engineering class and are working on a Vex Robot, please request access to pos...
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VEX Robot's Resource Page If you are in my Mechatronics Engineering class and are working on a Vex Robot, please request access to pos...
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I figured that the Dewey claw we are using isn't strong enough to open the mailbox. It just slips off. I plan to make a 3-D printed hook...
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During this time I created an outline of issues and their solutions in the Dewey engineering notebook. 1st Issue: Inaccessible cortex Dur...
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