During testing, the arm of Dewey was too short to reach within the mailbox.
Our solution to do this is to extend the arm of Dewey so that it could reach within the mailbox.
The other thing we are going to do is to change the controls of Dewey so it becomes easier to control.
The battery chamber is also pretty loose as well which would get fixed soon.
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Dewey - Tell Me About Your VEX- Pinned Post
VEX Robot's Resource Page If you are in my Mechatronics Engineering class and are working on a Vex Robot, please request access to pos...
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I figured that the Dewey claw we are using isn't strong enough to open the mailbox. It just slips off. I plan to make a 3-D printed hook...
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During this time I created an outline of issues and their solutions in the Dewey engineering notebook. 1st Issue: Inaccessible cortex Dur...
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VEX Robot's Resource Page If you are in my Mechatronics Engineering class and are working on a Vex Robot, please request access to pos...
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